Hmm .. well, 150 is close enough to 147.5 to make no difference ...
Mid section is off and getting the blow-lamp treatment to burn out as much as possible. Seems to be quite heavy and fouled, rear section has been cleaned up, didnt make any difference, doubt it would really, as its all a straight through pipe in effect. Carbs been off, looks clean as a whistle ... I'll wash the filter next.
I suppose it could be a damaged choke seal, it feels too rich to be down to a needle, and anyway, its still rich at fully open, the needle only affects 1/4 to 3/4 throttle, at wide open its all on the main jet. But, I'll check its on middle clip postion.